Brake Master Cylinders

After a brake master cylinder was installed, the technician was unable to bleed the brake system. Fluid pulled from reservoir would return to reservoir through the same line as the internal bypass was not functioning properly. Master cylinder was disassembled and bypass was found stuck and unable to move. Metal shavings were found inside, and an O-ring was torn, with black specks mixed in with the shavings. Part replaced with new master cylinder.

Gemini Sparkle

Key Takeaways:

  • Aircraft brake master cylinders exhibit diverse failure modes, consistently leading to reduced or complete loss of braking capability.
  • Common issues include internal mechanical failures (e.g., stuck bypasses, unthreaded glands, sheared piston rods), contamination from O-ring degradation or metal shavings, and external mechanical failures such as sheared cotter pins.
  • These failures can stem from component wear, inadequate part strength, or improper assembly and adjustment, underscoring the critical need for thorough inspection and maintenance.
See a mistake? Contact us.

BEECHCRAFT C90GT KING AIR

Unserviceable Component

After a brake master cylinder was installed, the technician was unable to bleed the brake system. Fluid pulled from reservoir would return to reservoir through the same line as the internal bypass was not functioning properly. Master cylinder was disassembled and bypass was found stuck and unable to move. Metal shavings were found inside, and an O-ring was torn, with black specks mixed in with the shavings. Part replaced with new master cylinder.

Part total time: 0.0 hours


CESSNA TU206G TURBO STATIONAIR

Sheared Shaft

The pilot lost right brake capabilities. Initial examination revealed brake master cylinder piston rod (p/n 0541143) was broken below its clevis check nut (p/n 0541140). Closer inspection found the clevis and check nut to have been bottomed out on the piston rod, causing contact with the right rudder/brake pedal shaft attachment horn. This condition caused the shaft to shear below the check nut and the sequential loss of brake capabilities.

Part total time: 5661.0 hours


CESSNA 208B GRAND CARAVAN

Failed Brake System

After landing, there was no response when pilot applied left brake. Engine reverse thrust was used to stop the aircraft, and the left brake started working after being pumped several times. Maintenance technicians inspected and troubleshot the brake system and ended up replacing the left brake master cylinder with a serviceable unit. Brakes and master cylinder (p/n 26820011) were bled and ops checks were good.

Part total time: 348.0 hours


CESSNA 425 CORSAIR/CONQUEST I

Worn Brake System

The pilot reported a “spongy” left brake and reduced braking capability. The master cylinder was disassembled and appeared to have black O-ring material contaminating its fluid. The master cylinder was cleaned, inspected and repacked with new O-rings.

Part total time: 10,877.0 hours


DIAMOND AIRCRAFT DA20-C1

Sheared Cotter Pin

Pilot reported the brakes were not working well. Maintenance found that the cotter pin, holding the bottom of the brake master cylinder (p/n 1054A) on the pivot shaft, had been sheared off, allowing the brake cylinder to move sideways and bind. The cotter pin (MS24665-24) is extremely light duty and perhaps not heavy enough for the application.

Part total time: Unknown


PIPER PA-46-310P MALIBU

Unthreaded Gland

On landing rollout, pilot had no left brake. Left brake master cylinder was removed and the end gland was found with all but two threads unthreaded, causing fluid and pressure loss from the master cylinder. Replaced internal seals, reassembled and reinstalled.

Part total time: 3076.0 hours

Ready to Sell Your Aircraft?

List your airplane on AircraftForSale.com and reach qualified buyers.

List Your Aircraft
AircraftForSale Logo | FLYING Logo
Pilot in aircraft
Sign-up for newsletters & special offers!

Get the latest stories & special offers delivered directly to your inbox.

SUBSCRIBE