Frayed, Stuck, Cracked

This aircraft has factory-installed, extended range fuel tanks, a “wet wing” design in each wing tip. These tanks were found leaking through the fuel vent tubes (p/n 60-170010) on both sides. The cause of the leak was found to be the deterioration of the sealant around the tube slip-joint fittings.

The DA62 uses a version of the E4 engine marketed as the AE330. Florian Pfaffstaller
Gemini Sparkle

Key Takeaways:

  • Deteriorated fuel tank sealant in a Beech Baron caused leaks and debris to contaminate the fuel system.
  • A routine inspection on a Cessna Grand Caravan revealed a flap cable with 30 percent of its strands broken.
  • Improperly securing the control yoke with a seat belt in high winds led to damaged elevator mount brackets on a Cessna Titan.
  • A Piper Seminole experienced an in-flight emergency due to a stuck throttle cable, and a Continental engine was found with a cracked crankshaft at the propeller flange.
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Beech Model 58 Baron
Fuel Tank Sealant Deterioration

This aircraft has factory-installed, extended range fuel tanks, a “wet wing” design in each wing tip. These tanks were found leaking through the fuel vent tubes (p/n 60-170010) on both sides. The cause of the leak was found to be the deterioration of the sealant around the tube slip-joint fittings.

Present in the tanks was an excessive amount of debris, deteriorated fuel tank sealant. These particles were trapped in multiple locations throughout the entire fuel storage system with no way of detecting their presence.

Part Total Time: (unknown)

Cessna 208B Grand Caravan
Frayed Flap Cable

During a routine inspection, the flap cable (p/n 2660001105) from the inner bell crank to the outer end of the flap was found frayed at the fairlead. About 30 percent of the strands were broken. This cable was original and, judging from the slip mark, the cable had not (moved from its swaged fitting.

Part Total Time: (unknown)

Cessna 404 Titan
Damaged Elevator Mount Brackets

While this aircraft was tied down, its control yoke was secured in the full-aft position with a seat belt instead of the approved gust lock device. This allowed the elevators to move and high winds caused the elevator to hammer its lower stop until the bracket’s upper mounts failed. All pre-flight checks were normal. It was not until the control surface incurred air loads that the problem was discovered and the takeoff aborted.

Part Total Time: (unknown)

Piper PA-44-180 Seminole
Stuck Throttle Cable

The aircraft’s l/h engine throttle lever stuck at 25 inches of manifold pressure during multiple landing operations. After departing the pattern, the crew was able to reduce power and, on recommendation from ground-based maintenance personnel, secured the engine, declared an emergency and uneventfully performed a single-engine landing.

Although there is no speculation on causes for the cable (p/n 554546) binding, there have been previous reports of problems with engine control cables installed in this make and model aircraft.

Part Total Time: 705.0 hours

Continental IO-520-C
Cracked Crankshaft

The crankshaft (p/n 649859) cracked in the propeller flange at the radius. The crack appeared in a “V” shape. On one side, the crack was about four inches long, and on the other about three inches.

Part Total Time: 4531.0 hours

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