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AMOC For Cessna 150/152s

During an annual inspection, technicians found the l/h elevator balance weight (p/n 96-610022-7) detached from its mount. The r/h elevator balance weight was found both broken and loose on its mount. The detached l/h weight was able to shift position inside the elevator and cause an out-of-balance condition. This damage appears to be caused by vibration.

Gemini Sparkle

Key Takeaways:

  • Several aircraft reported structural integrity issues, including loose elevator balance weights on a Beechcraft B58 Baron, a cracked wing spar attach fitting on a Beechcraft 200 King Air, and severe corrosion under a spar attach fitting on a Piper PA-28R-180.
  • A Lycoming turbocharger failed on a Piper PA-28, leading to smoke and internal fire due to a main bearing failure.
  • The FAA issued a Global Alternate Method of Compliance (AMOC) for AD 2011-10-09, permitting specific repairs to steel seat foot/roller housings on Cessna 150/152 airplanes.
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Beechcraft B58 Baron
Loose Elevator Balance Weights

During an annual inspection, technicians found the l/h elevator balance weight (p/n 96-610022-7) detached from its mount. The r/h elevator balance weight was found both broken and loose on its mount. The detached l/h weight was able to shift position inside the elevator and cause an out-of-balance condition. This damage appears to be caused by vibration.

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