My Ditching

The NTSB’s factual report is succinct: “The pilot stated that, about 30 minutes into the flight, he was over the water about 15 miles to the nearest land, when the engine experienced a total loss of power.

Gemini Sparkle

Key Takeaways:

  • A pilot experienced a total loss of engine power about 30 minutes into a flight over water.
  • After unsuccessful restart attempts, the pilot initiated an emergency descent, circled a private vessel, and ditched in the water nearby.
  • The pilot and passenger safely exited the airplane before it sank and were rescued by the private vessel.
  • The probable cause of the engine power loss could not be determined because the airplane was not recovered.
See a mistake? Contact us.

The NTSB’s factual report is succinct: “The pilot stated that, about 30 minutes into the flight, he was over the water about 15 miles to the nearest land, when the engine experienced a total loss of power. The pilot made several attempts to restart the engine, each of which was unsuccessful; he subsequently initiated an emergency descent. The pilot circled a private vessel during the descent and ditched in the water nearby. He and his passenger exited the airplane before it sank and they were picked up by the vessel. The airplane was not recovered.”

The probable cause finding: “A total loss of engine power during cruise flight for reasons that could not be determined because the airplane was not recovered.”

The chart excerpt above details the route I was flying; the “x” marks the spot of my ditching. At right is a photo of my first flight in the airplane, a Jabiru-powered Texas Sport Cub I built from a kit.

Ready to Sell Your Aircraft?

List your airplane on AircraftForSale.com and reach qualified buyers.

List Your Aircraft
AircraftForSale Logo | FLYING Logo
Pilot in aircraft
Sign-up for newsletters & special offers!

Get the latest stories & special offers delivered directly to your inbox.

SUBSCRIBE