Jammed And Frayed

The control yoke was binding when turned left approximately 45 degrees. Upon inspecting the aileron control system, a screw was found lodged in a pulley groove and the cable (p/n 106-524044-19) was damaged. The aircraft had flown 2.0 hours since its last annual inspection. The screw appeared to be a floor panel screw.

Gemini Sparkle

Key Takeaways:

  • Aircraft control systems experienced critical failures, including an aileron cable jammed by a loose screw and other frayed aileron cables potentially due to pulley wear, along with sheared elevator actuator rivets.
  • Engine components displayed significant wear and damage, such as a cracked exhaust valve leading to power loss and a fractured turbo-exhaust clamp.
  • Additional issues involved a leaking oil/fuel heater tube suspected to be caused by chafing and corrosion, indicating material fatigue in critical lines.
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Beechcraft A36 Bonanza

Jammed Aileron Control Cable

The control yoke was binding when turned left approximately 45 degrees. Upon inspecting the aileron control system, a screw was found lodged in a pulley groove and the cable (p/n 106-524044-19) was damaged. The aircraft had flown 2.0

288

hours since its last annual inspection. The screw appeared to be a floor panel screw.

Part Total Time: 2266.3 hours.

Cessna 172S Skyhawk

Frayed Aileron Control Cables

Flat spots and fraying were noticed on three aileron control cables (p/ns 0510105-365, -364, -360). A substantial groove could be seen in the carry-through cable. Cable tensions were within specification. The plastic pulleys were clean and free to roll.

The submitter speculates the wear results from the cables rubbing against the pulleys instead of rolling, and suggests replacing them with the phenolic pulley used in all other areas of the aircraft.

Part Total Time: 2096.7 hours.

Cessna 208B Grand Caravan

Leaking Oil/Fuel Heater Tube

The ridged steel tube feeding the oil/fuel heater developed pin holes underneath the attached fire loop bracket. When this line (p/n: 3013446) is removed, the pin holes look like little dots of corrosion, but when pressurized it leaks at an extreme rate. A possible cause could be Adel clamp chafing.

Part Total Time: (unknown)

Piper PA-46-350P

Sheared Elevator Actuator-Arm Rivets

An inoperative elevator trim was found to be caused by a frayed cable jamming the trim drum. The elevator actuator arm (p/n 83515-02) was loose and free to move in all directions. All but one actuator arm-to-elevator rivets were sheared or loose. Jet blast or severe wind is believed to have caused the elevator to hit the stops with damaging force.

Part Total Time: 2995.0 hours.

Continental GTSIO520-H1

Cracked Turbo-Exhaust Clamp

During an annual inspection the clamp between the turbocharger and exhaust (p/n: NH1000897-50) was found with a 4.5-inch crack along its circumference.

Part Total Time: (unknown).

Continental IO-550-B

Cracked Exhaust Valve

The engine experienced power loss, vibration and low number 2 exhaust gas temperature. Upon inspection, the number two cylinder exhaust valve (p/n 646286) was found to be missing about half its face.

Part Total Time: 830.0 hours

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